• You Know You're Having A Bad Day When . . .
Immediately after take-off, the #4 alternator would not stay in parallel with the other three alternators, so it was taken off-line and de-excited three minutes into the flight. About one minute after the #4 alternator was shut down, flames 8 to 12 feet long erupted from around the air plug of the number-one engine. The left scanner reported the flames to the pilot. Six minutes after take-off, the flight engineer shut down the number-one engine, feathered its propeller, and expended one of its methyl bromide fire extinguishing bottles.
The mission continued on the power of the remaining five engines. 44-92035 cruised to the gunnery range on Matagorda Island at an altitude of 5,000 feet. It arrived at 7:00 A.M. and the gunners began practicing. Radar Observer S/Sgt. Ray Earl manned the tail turret. The charger for the right gun burned out, so he expended just half of his ammunition. Then the APG-3 radar for the tail turret started acting up, so S/Sgt. Earl secured the set.
Aircraft Commander 1st Lt. Oliver Hildebrandt noted that the vibration from firing the 20mm cannons increased significantly during the fourth gunnery pass. Immediately afterward, radar operator Captain James Yeingst notified Hildebrandt that the APQ-24 radar set blew up and was smoking. Vibration from the firing of the guns was causing shorting between the internal components of the radar. Then the liaison transmitter failed as well.
The cannons in the left forward upper turret and the left rear upper turret stopped firing. The gunners attempted to retract the gun turrets, but the failed turrets would not retract. Gunner S/Sgt. Fred Boyd entered the turret bay, but other problems began to take precedence over the stuck turrets. Boyd was called out of the bay before he could manually crank the turret down.
At 7:31 A.M. the number-three engine suffered an internal failure. The torque pressure fell to zero. The manifold pressure dropped to atmospheric pressure. The fuel flow dropped off, and the flight engineer could not stabilize the engine speed. The pilot shut down the number-three engine and feathered its propeller. The B-36B had only one operating engine on the left wing, so the pilot aborted the remainder of the training mission and set course for Kelly Air Force Base.
Flight engineer Captain Samuel Baker retarded the spark, set the mixture controls to "normal", and set the engine RPMs to 2,500 to increase the power from the remaining engines. Unknown to Captain Baker, the vibration from the guns had disabled the electrical systems controlling the spark settings and fuel mixture. He immediately discovered that the turbo control knobs no longer affected the manifold pressure.
The B-36B could not maintain its airspeed on the power of the four remaining engines. It descended about 1,000 feet and its airspeed bled off to 135 miles per hour. The pilot called for more power. The flight engineer attempted to increase engine speed to 2,650 RPM and enrich the fuel mixture, but got no response from the engines except for severe backfiring. The fuel mixture indicators for all of the engines indicated lean.
The second flight engineer, M/Sgt. Edward Farcas, checked the electrical fuse panel. Although the fuses appeared to be intact, he replaced the master turbo fuse and all of the individual turbo fuses. He noticed that the turbo-amplifiers and mixture amplifiers were all cooler than normal. He climbed into the bomb bay to check the aircraft power panels and fuses, but could not find any problem there.
Kelly Air Force Base had a cloud overcast at just 300 feet and the visibility was restricted to two miles. The weather at Bergstrom Air Force Base not as bad, with scattered clouds at 1,000 feet, broken clouds at 2,000 feet and 10 miles visibility. Carswell Air Force Base was clear with 10 miles visibility, but it was 155 miles farther away than Bergstrom. Air traffic control cleared all airspace below 4,000 feet ahead of the crippled B-36B. Aircraft Commander Hildebrandt was flying on instruments in thick clouds.
The poor weather at Kelly Air Force Base convinced Hildebrandt to change course from Kelly to Carswell Air Force Base, passing by Bergstrom Air Force Base on the way in case the airplane could not make it to Carswell. Bombardier Captain Robert Nelson made two attempts to salvo the 1,500 pounds of practice bombs in the rear bomb bay, but the bomb bay doors would not open by automatic or manual control, or emergency procedure.
There was no way to dump fuel to reduce the weight of the B-36B. The flight engineers resorted to holding down the switches used to prime the fuel system in an attempt to increase fuel flow to the engines.. M/Sgt. Edward Farcas held down the prime switches for the number-two and number-four engines while Captain Baker held down the prime switch for the number-five engine and operated the flight engineer's panel. The configuration of the switches did not allow them to prime the number-five engine and the number-six engine at the same time.
The high power demand coupled with the lean fuel mixture made the cylinder head temperatures of the engines climb to 295 degrees C. Flight engineer Baker jockeyed the throttles, decreasing the throttle setting of the engine with the highest cylinder head temperature until another engine grew even hotter. The high temperature caused the gasoline/air mixture in the cylinders to detonate before the pistons reached top dead center, diminishing power and damaging the engines.
Despite the critical situation with the engines, Aircraft Commander Hildebrandt decided to continue past Bergstrom Air Force Base to Carswell. Bergstrom was overcast and its runway was only 6,000 feet long. Carswell offered a much longer runway. By the time the B-36B reached Cleburne , the backfiring on all engines increased in violence. The number-2, number-5, and number-6 engines were running at 70% power and the number-4 engine was producing only 20% power. The airspeed had dropped off to 130 miles per hour.
Aircraft Commander Hildebrandt attempted to restart the number-one engine, the one that had spouted flames on take-off, but fuel was not getting to its induction system.. He tried to restart the number-three engine, but could not unfeather the propeller on that engine. As the bomber passed to the west of Cleburne , the right scanner reported dense white smoke, oil, and metal particles coming from the number-five engine.
After a short while the number-five engine lost power, and Aircraft Commander Hildebrandt feathered the propeller on that engine while still twenty-one miles from Carswell Air Force Base. The B-36B could not stay airborne on the power of the three remaining failing engines. It was flying at just 125 miles per hour, seven miles per hour above the stall speed, losing both altitude and airspeed. Howard McCullough and W. Boeten were flying Civil Aeronautics Authority DC-3 N342 near Cleburne . They were notified by Meacham Tower to be on the lookout for 44-92035. They spotted it about five miles south of Cleburne . They observed that the number-one and number-three propellers were feathered and the number-five engine was on fire. They turned to follow the descending bomber Aircraft Commander Hildebrandt ordered the crew to bail out of the stricken bomber.
Bombardier Captain Robert Nelson had bailed out of airplanes on two previous occasions. He had crash landed twice and ditched once. He was the first man to bail out from the forward crew compartment. He suffered contusions of his lower spine when he landed.
Radar Operator Captain James Yeingst responded to stress with laughter and jokes. He was a bit giddy before the bailout. He was the second man to exit from the forward crew compartment. His parachute streamed after he pulled the rip cord. He passed Captain Nelson going down. Captain Yeingst's parachute mushroomed open just before he hit the ground, but he suffered fatal injuries.
Co-pilot Captain Wilbur Evans was the third man to exit from the forward crew compartment. He had bailed out of airplanes twice before and crash landed several times during WW-II. This time he broke both bones in his lower right leg when he landed.
Navigator Captain Horace Stewart had previously tried to get off flying status because he felt that the B-36 was too dangerous. It is reported that during the hour before bailout, he was tense, nervous, and chain-smoking. He was the fourth man to bail out from the forward crew compartment. He pulled his rip cord right as he exited the forward escape hatch on the left side of the fuselage. His parachute opened and pulled him toward the number three propeller. His head hit the downward pointing blade of the propeller, killing him instantly.
Radio Operator Cpl.. Paul Myers followed Captain Stewart out the escape hatch. Myers landed with minor injuries. Flight Engineer M/Sgt. Edward Farcas jumped head first through the exit hatch of the forward crew compartment right after Cpl. Myers. His parachute did not open when he pulled the rip cord. He pulled the parachute out of its pack with his hands and landed with only minor injuries.
Radar Mechanic Robert Gianerakis and Flight Engineer Captain Samuel Baker were the next to escape from the forward compartment. Both landed with only minor injuries. Radio Operator Sgt. Armando Villareal bailed out after Captain Baker. Villareal did not trust his parachute to open, so he pulled the rip cord while he was still in the forward crew compartment.. He held his parachute in his arms as he jumped feet first through the escape hatch. Despite his unorthodox method of escape, he landed with only minor injuries.
Pilot 1st Lt. Walter Ross was the next to last to leave the forward compartment. He landed with only minor injuries. Gunner S/Sgt. Andrew Byrne and Radar Observer S/Sgt. Ray Earl were the first two crew members to bail out of the rear crew compartment. Both landed with only minor injuries. Gunner Cpl. Calvin Martin was the third man to exit the rear crew compartment. He was swinging under his parachute as he hit the ground. He broke his right ankle as he landed. He fell backward onto a rock, fracturing his third lumbar vertebra and compressing his tailbone.
Gunner S/Sgt. Ronald Williams followed Cpl. Martin out the rear escape hatch. He landed with only minor injuries. Gunner S/Sgt. Fred Boyd was the last man to exit the rear crew compartment. He called to Aircraft Commander Hildebrandt over the intercom to let him know that everyone had escaped from the aft compartment. When he turned back to the exit hatch, it had fallen shut. He had to open the hatch again to make his escape. He broke the fibula of his left leg when he landed farther to the north than the other crew members.
After S/Sgt. Boyd reported that all other crew members had bailed out of the rear compartment, Aircraft Commander Hildebrandt set the autopilot and jumped clear when the bomber was less than 1,000 feet above the ground. He and nine other crew members escaped from the B-36B with only minor injuries. When McCullough and Boeten in DC-3, N342 saw the parachutes of the escaping crew members, they announced the bail-out on the emergency frequency of 121.5 megacycles.
Each report of Emergency Parachute Jump indicates that the incident occurred 20 miles south southeast of Carswell Air Force Base. The descent of the B-36B was witnessed by Mr. Buck Bell and his wife, who lived about 5 to 7 miles southwest of Crowley, Texas. Mr. Bell saw the crew members parachuting from the bomber, but did not see it hit the ground about one mile north of his house. Mr. James Bandy and his wife were on the road to Cleburne about 4 miles from their house on Route 1 near Joshua when they spotted the B-36B trailing smoke, flying in a nose-high attitude. They saw it hit the ground in a level attitude, raising a cloud of dust.
The B-36B descended straight ahead in a nose-high attitude for a mile after Aircraft Commander Hildebrandt bailed out. It stalled, pitched nose down, and impacted in a terraced field on Less Armstrong's Dairy, 14 miles south of Carswell Air Force Base, 2 miles west of the South leg FTW range, and six miles west of Crowley at 9:50 in the morning. The forward crew compartment separated and folded underneath the rest of the fuselage. The tail section broke off, and the rear crew compartment came away from the mid-fuselage as the wreckage slid 850 feet along the ground and twisted to the right.
The rear sections of the airplane remained largely intact. The elevation at the crash site was approximately 700 feet. Mr. W. Doggett witnessed the bail-out and crash from his home on Route 1 near Joshua. The B-36B impacted about 2-1/2 miles north of his house. He drove to the crash site in his pickup truck and helped the surviving crew members to regroup.
Four minutes after the crash, McCullough and Boeten in DC-3, N342 reported that two Navy aircraft were circling the wreckage. The wreckage smoldered for about eight minutes before a fire broke out in the number-six engine. The 15,000 gallons of remaining fuel consumed the forward fuselage and wings. The civilians and crew members were driven away from the crash site by exploding ammunition and the knowledge of the presence of 1,500 pounds of bombs aboard the airplane.
Labels: B-36, convair, crash, peacemaker, USAF
• Blackberry Pilot
Is the guy in the right seat texting or checking his Blackberry ?
Naw, didn't think so. But the picture is good evidence why you shouldn't put loose items on the parcel shelf or seat behind you.
Labels: blackberry, crash
• Second Guessing Sully?
After watching the video of US Airways 1549 ditch in the Hudson, and after reading that controllers suggested they go to Teterboro, I wondered what the situation would have looked like to the pilot. So I cranked up Microsoft Flight Simulator X on my iMac (yes, Windows actually runs better on a Mac) to see what would have happened if Sully had gone to KTEB instead.
UPDATE: Also tried returning to KLGA Rwy 13. Added images below.
UPDATE: See info from Airbus pilots before the comments.
UPDATE: See what a goose does to a jet engine
UPDATE: A history of airline ditching with pictures
UPDATE: FAA transcript and audio from the flight are available here.
So I set the sim for January 15th, 2009 at 3:25PM and lined up a 160,000 pound (20,000 under gross wt) A320 on runway 4 at La Guardia.

One minute after takeoff at 3000' I shut down both engines. That's La Guardia under the aircraft in the distance (click images to enlarge).

As I turned west, Teterboro is a small white patch across the river, middle left in the windscreen, above the George Washington Bridge highway.

"We're too low," turning south just north of the GW bridge "We're gonna be in the river"

Seconds before splashdown

Splash, right at the 38th street pier. So the simulator model is accurate and produces the same result.

Here's the profile map

Now let's try for Teterboro and make it as easy as possible—no pax or cargo, minimum fuel, no worries about the steady stream of biz jets and GA traffic that would otherwise defintely be a factor. Same cut at 3000 feet, balloon to 4600' to reach best glide speed of 130 from 250kts climb speed. Over the river headed west, crossing the Hudson, it looks like it might work.

Modified base for Rnwy 24 Teterboro (6000 feet long), still looks do-able.

But after touchdown slightly long thanks to misjudging the tailwind (about 1000') and without reversers, we're off the end. So there may be a way with a light aircraft and better approach. 7000' Rnwy 19 is not an option because of the longer approach, Rnwy 1 worse yet for same reason and it requires an acute turn to final.

Now let's try it at 180,000 pounds, close to gross weight (Vr goes from 131 to 161, and so does best glide speed, I'll wager). Over the river it's not looking good, and the fly-by-wire system won't let me fly slower than 200, which is probably above best glide speed.

Headed straight for the airport, forget runway lineup. We're going to have to put it in the river (not the Hudson). Dumped the flaps and ended up well short (we hit the highway bridge and then went in the drink)

About 2 miles short.

Good call Sully!
Someone asked what woukd happen in the sim if we tried to go back to La Guardia and land on runway 13. Heavy it didn't work in 4 tries. Light (empty), I didn't make it the first time, but it was close. Next time it worked when I turned back almost immediately. Here's what it looked like on approach

And after landing

Here's the map

So once again—Good call Sully!
A new map from FAA with more detailed real life time/altitude/speed info (click to enlarge)

Reports state geese were flying at 2900'. This would imply that the A320 would have already cleaned up from its original take off flap setting (most likely config 1 which would have a small amount of flap on the trailing edge and a small amount of slat on the leading edge) to a clean configuration and acceleration to 250 kts indicated airspeed, the maximum permitted speed below 10,000' in the US.
The engines would have been in the 'climb gate' which means that the auto thrust system would be engaged with the FMGES (flight management, guidance and envelope system) computers able to automatically set thrust to whatever it requires between idle and approx 90% of the maximum continuous thrust.
The co-pilot was the pilot flying (PF) for this sector with the captain playing the pilot non-flying (PNF) support role (radios, monitoring, system selection, etc). On fly by wire (FBW) Airbuses (Airbii?) the autopilot can be engaged from the later of 100' or 5 seconds after take off but most of us like to play awhile so I don't know if it was engaged or if PF was hand flying at the time.
It would appear that on hitting the birds the power loss on both engines was instantaneous. I would expect that the flight deck would momentarily have gone dark with all the screens blank while the electrical system reconfigured itself onto battery power. During this time a small ram air turbine (RAT) would drop out from the underside of the aircraft with a freewheeling propeller that spins up to 6000ish rpm in the airflow.
Modern Airbus have 3 electrical systems referred to as the Green, Blue and Yellow systems (you can't afford to be colour blind in an Airbus!) with hydraulic dependent systems spread across these 3 providers to allow system redundancy. The engines have pumps attached that normally pressurise the 3 hydraulic systems to 3000 psi however these engines had now stopped so the RAT would supply hydraulic pressure at 2500 psi to the blue hydraulic system only. With only the blue system available the aircraft would have had both elevators but only the left aileron operational (the rudder is electric on the 320 so other redundancy caters for that). The loss of all the engine driven electrical generators would also cause the emergency generator to come on line. This is a small generator that is driven by blue system hydraulic pressure (effectively a windmill in the fluid lines) with enough output to power minimal flight instrumentation, flight control computers, FADEC's (computers governing thrust management), SFCC's (slat/flap control computers), etc, etc. The emergency generator means that the batteries can be saved for any future needs as they are only guaranteed for 30 minutes.
So at this point the aircraft has flight controls and limited electrics. There would then be the most awful buzz of aural warnings and illuminations as the aircraft then reports itself to the pilots as being unfit for use. If the autopilot was engaged it would have dropped out and as the only pilot instrumentation showing would be the captains PFD (primary flight display) and the ISIS (integrated standby instrument system) he would now become the PF while the co-pilot now became the PNF.
In normal circumstances Airbus flight guidance is unlike conventional aircraft as forward and backward movement of the sidestick does not directly control the elevators but does directly control g load demand. Lateral movement of the sidestick does not directly control the ailerons; it sends a request to the flight control computers for a desired roll rate. There are also flight envelope protections in place controlled by the flight control computers that prevent the aircraft exceeding preset pitch and bank angles, min and max speeds, min and max g loadings, etc and when all these are in place the aircraft is referred to as operating in 'Normal Law'. There are another 6 'laws' that the aircraft can fly under (alternate 1, alternate 2, flare, abnormal attitude, mechanical backup) including the reversionary mode the aircraft would have dropped into in this case, 'Direct Law'. In this mode the sidestick movement is effectively directly related to aileron and elevator movement and in effect the aircraft has downgraded itself 3 stages to handle the same as a normal aeroplane. We even have to start trimming!
The aircraft appears to have reached a max alt of 3200' before transitioning to the glide. The Captain is now handflying and will also have taken over the radios while the FO now has the job of dealing with the systems and failures. The Airbus has a system called ECAM (electronic centralised aircraft monitoring) which not only displays normal aircraft system information on 2 screens in front of the pilots in the middle of the panel but also automatically presents checklists and operation procedures during failures scenarios. The upper ECAM screen would be awash with pages and pages of procedures for him to work through however the aircraft
will prioritise the failures and put the engine relight procedures at the top of the list
The ECAM would instruct him to:
1 – Switch on the engine igniters. Jet engines operate with the 'spark plugs' normally switched off as they are a constantly burning fire unlike a piston engine. Relight
will not happen without a spark though.
2 – Return the thrust levers to idle for correct fuel delivery during start sequence.
3 – Request PF to fly at 280kts which is the optimum speed for relight. In light of the low altitude I very much doubt they would have wanted to do this. If they had they would have needed a target pitch attitude of approx 2.5 degrees nose down and assuming a weight of 70 tonnes in still air the glide would have been 2.6nm per 1000'. I suspect the captain would in fact have come back to 'green dot' speed for improved gliding range. Green dot speed is computer generated and displayed as a green dot on the speedtape on the PFD and shows you the exact speed for max lift/drag ratio for that weight in the ambient conditions in the current configuration. I would hazard a guess that on a little Airbus (minibus!?!) this would be just over 200 knots.
4 – Select the emergency generator manually on in case the system has not come on automatically.
5 – Use number 1 VHF or HF radios and Transponder as only those are powered in emergency electrical configuration.
6 – Reset number 1 Flight Augmentation Computer allowing recovery of the electrical rudder trim as the unpowered right aileron would now start to float up hampering control further.
7 – If no engine relight after 30 seconds then engine master switches off for 30 seconds to purge the combustion chambers before restarting the ignition sequence. Below FL200 the APU can be used to assist with engine starting however even if the APU had been running it would not be able to be used within 45 seconds of loss of engine driven generators to prevent interference with emergency generator coupling.
At some point the crew would then have to accept their fate that the engines are unlikely to restart and transfer to the Ditching checklist which is not on ECAM but would have to be accessed from the QRH (quick reference handbook) located to the side of each pilot.
Now the FO had a new list of jobs to perform:
1 – Prepare cabin and cockpit. Ensure cabin crew are notified and doing their thing, secure loose items in the cockpit, prepare survival equipment, tighten harness and select harness lock, etc..
2 – Switch GPWS (ground proximity warning systems) and EGPWS (enhanced GPWS) systems off so that the aircraft does not start shouting 'Too Low Gear' or 'Whoop Whoop Pull Up' at you when you are trying to concentrate on a tidy crash.
3 – Seatbelt signs on. Somehow think this one got into the checklist to appease the lawyers at the subsequent board of enquiry!
4 – Turn off cabin and galley electrical power.
5 – Select landing elevation to zero on pressurisation control panel as this would currently be set to the landing elevation at the planned arrival airfield. If the aircraft
was still pressurised on ditching it might not be possible to open the doors.
The QRH advises the crew to ditch with the gear retracted and the flaps set to the max available setting (normally called Config Full). On the A340 we can achieve Config Full as our RAT supplies the Green hydraulic system. However, looking through the A320 manuals where the RAT supplies the Blue system I can only see a capability to deploy the leading edge slats only. It would be possible to get Config Full by manually switching on the Yellow system electric hydraulic pump to pressurise the Yellow system and then via a PTU (power transfer unit) the Green system would also be powered but this is not SOP so I suspect the aircraft may have ditched with slats deployed and flaps retracted but don't take that as gospel.
At 2000'agl the FO then:
1 - Check that the cabin pressurisation mode selector is in AUTO.
2 – Switch all engine and APU bleed valves off.
3 – Switch on the overhead 'DITCHING' pushbutton. The outflow valve, the emergency ram air inlet, the avionics ventilation inlet and extract valves, the pack flow control valves and the forward cargo outlet isolation valve all close to slow the ingress of water.
At
1000'agl the FO then:
1 – Makes 'Cabin crew seats for landing' PA.
At
200'agl the FO then:
1 – Makes 'Brace for impact' PA.
At touchdown the FO then:
1 – Engine master switches off.
2 – APU master switch off.
After ditching:
1 – Notify ATC.
2 – Press all engine and APU fire pushbuttons to arm fire extinguisher squibs and isolate fuel, hydraulic, pneumatic and electrical couplings.
3 – Discharge all engine and APU fire extinguishers.
4 – Initiate evacuation.
I have left out a lot of the explanatory text from the QRH for brevity but you can see that this is an almighty amount of work to achieve in an ultimate pressure scenario. I have not even touched upon the proper evacuation checklist. I have also done Monsieur Airbus an injustice but drastically simplifying my explanations of the key systems in an attempt to make them more understandable but I hope it is of interest to those that made it to the end of the text!
In my company we do practice this event in the simulator for both ditching and crash on land. In fact I last did a 4 engine inop landing in the simulator just 6 months ago having simulated a departure from Tokyo followed by a volcanic ash ingestion at FL250 in the climb leading to 4 engine flame out with unsuccessful relight attempts. We ran the exercise twice and both times managed to successfully glide back to Tokyo with the only damaged being burst main wheels from hammering the brakes. We practice many, many other horrendous scenarios (such as flying the aircraft to successful airport landings with the loss of all power to the flight control surfaces) so you can see that the only subjects that we are not prepared for are the ones we haven't thought of yet.
Hats off to the entire crew for a most amazing job done brilliantly and top marks to Airbus for showing all the doubting Thomas's that they were so very wrong about the strength of the aircraft.
Comments on the above from another Airbus driver:
The Airbus in everyday operation is a wonderful aeroplane and makes the job easy, unfortunately its when things start to go wrong that it makes life difficult for you. What the description of events doesn't really convey is the time frame across which all this happens.
During the climb they would have heard a couple of large bangs as the birds were ingested and a very noticeable drop in engine note. They would have immediately looked at the engine indications on ECAM realising they have lost power from both engines, a second or two later the whole cockpit would have gone dark with some clunking noises, losing all screens and no matter how brief this is, its always scary! A second or two later just the Captain's screens would have come back and simulatneaously the autopilot would drop out with the audible cricket warning (The Airbus philoshopy is if you have a double failure 'you have control', just when you need the extrra capacity you have to fly it too) . ECAM would be going spare 'binging' away in a panic flicking through drills prioritising them, so for a short while you can't do anything as the screen keeps changing. All in a matter of seconds. If they were just over 3000' when this occured they had just over three minutes before splash down. Not long to pull yourself together, realise your not going to make the airfield ahead, decide on the river, remember the appropriate drill in the QRH, get your FO to start carrying them out and configure for a ditching.
Added to this they had a problem with the cabin crew. After any incident the flight deck will give the cabin crew a NITS brief) Nature of the problem, our intentions, the time frame to landing and any special considerations for their duties) The trouble is they had just taken off, as soon as the wheels are up the cabin crew are released for duties and whats the first thing they do? They get on the PA and try to sell you shite you dont want. So our man couldn't contact the crew or the passengers to tell them what is going on. (A good argument I think to reduce the annoying number of unneccessary sales PAs on flights) No doubt a certain amount of his last three minutes were spent trying to break through the sales crap to announce to everyone that they were making a forced landing. While flying the aeroplane and making the Mayday calls (as only his radio worked.)
Apparently the Captains CV is a thing to behold and well worth looking up, if ever there was a suitable man to be flying that plane that day it was him. There is no doubt that they both did an amazing job and I just wonder if it had been Ryan air, with a 2500 hr Captain and a 200 hour Eastern European First Officer would the outcome have been the same? I doubt it.
Labels: A320, crash, hudson, La Guardia, LaGuardia, Scully, US Airways